The
Accident near Brehliu in 1946
The poor standards of maintenance caused by the second world war left
the entire infrastructure and stock of the RSR in a severely run-down
state. Particularly badly affected were the track and locomotives with
inside cylinders. This parlous state of affairs, or rather a lack of
attention to it on the part of RSR staff, was the direct cause of a
serious accident on 3rd February 1946. A goods train, hauled by the
delapidated Teslov 3-cylinder 2-8-4 no. 433C.019
and consisting of over
sixty two-axled wagons, was descending the gradient from Lihnoprun to
Brehliu at the somewhat reckless speed of 85 km/h, when the inside
crankpin bearing seized and caused the connecting rod to shear off just
in front of the big end. The inside cylinder, still of course being
supplied with steam by the valve gear, flailed the broken connecting
rod back and forth once or twice, until it punctured the underside of
the boiler, engulfing the engine in a great cloud of steam and hot
water. The crew were taken completely by surprise and the driver
instinctively made an emergency brake application. The rickety goods
wagons, many with less than effective brakes, soon found their way off
the uneven track and turned away to both sides, some spilling down the
embankment over which the train was just passing and some crossing over
to the opposite track.
At that moment, as fate would have it, an eight-coach express from
Gunerad to Forihv, hauled by the freshly outshopped Šahlmeti
4-6-0 no.
323C.021, was forging up the gradient at
some 55 km/h and ran head-on
into the wayward wagons. The express was brought almost to a dead stop,
the front bogie of no. 323C.021 being derailed and the first two
coaches telescoping against the tender; the third coach of the express
leaned over and was strafed by a couple of the wagons which had till
that moment held the track.
The crew of the express were both injured and in the telescoped coaches
nine people were killed and twenty-three more injured, some seriously.
Many other persons suffered cuts and bruises. The third coach of the
express was damaged on its corridor side, affording the passengers a
fortunate escape.
The public enquiry, held as usual in the Bevice City Courthouse on 4th
April 1946, apportioned considerable blame to the crew of the goods
train, who were found to have driven at excessive speed in view of the
poor mechanical condition of their locomotive and the generally bad
state of the permanent way. In defence the driver stated that a
knocking big end was a sign of a loose bearing, not of one that was
about to seize up, and was in any case typical of class 433C
locomotives. It is also relevant to speculate what the ride must been
like on the footplate of no. 433C.019, bearing in mind the bad state of
the track and that class's reputation for rough riding. (This was a
factor in the decision to rebuild the engines into 2-8-2s in
1950.) In the main, however, the crash was designated a misfortune of
war by the enquiry and led to the recording of verdicts of accidental
death on the victims at the coroner's court in June 1946.
Locomotive no. 433C.019 became no. 433E.019
in November 1950 and
remained in service until October 1966. No. 323C.021 went to the
scrapyard in March 1954.
(c) Norman Clubb 2004